When the driver ran out of DMA chaining buffers, it kept the timeout for
the I/O, and I/O would stall.
The driver was not freezing the device queue on errors.
mps.c: Pull command completion logic into a separate
function, and call the callback/wakeup for commands
that are never sent due to lack of chain buffers.
Add a number of extra diagnostic sysctl variables.
Handle pre-hardware errors for configuration I/O.
This doesn't panic the system, but it will fail the
configuration I/O and there is no retry mechanism.
So the device probe will not succeed. This should
be a very uncommon situation, however.
mps_sas.c: Freeze the SIM queue when we run out of chain
buffers, and unfreeze it when more commands
complete.
Freeze the device queue when errors occur, so that
CAM can insure proper command ordering.
Report pre-hardware errors for task management
commands. In general, that shouldn't be possible
because task management commands don't have S/G
lists, and that is currently the only error path
before we get to the hardware.
Handle pre-hardware errors (like out of chain
elements) for SMP requests. That shouldn't happen
either, since we should have enough space for two
S/G elements in the standard request.
For commands that end with
MPI2_IOCSTATUS_SCSI_IOC_TERMINATED and
MPI2_IOCSTATUS_SCSI_EXT_TERMINATED, return them
with CAM_REQUEUE_REQ to retry them unconditionally.
These seem to be related to back end, transport
related problems that are hopefully transient. We
don't want to go through the retry count for
something that is not a permanent error.
Keep track of the number of outstanding I/Os.
mpsvar.h: Track the number of free chain elements.
Add variables for the number of outstanding I/Os,
and I/O high water mark.
Add variables to track the number of free chain
buffers and the chain low water mark, as well as
the number of chain allocation failures.
Add I/O state flags and an attach done flag.
MFC after: 3 days
the controller firmware will return all of our commands. Instead, keep
track of outstanding I/Os and return them to CAM once device removal
processing completes.
mpsvar.h: Declare the new "io_list" in the mps_softc.
mps.c: Initialize the new "io_list" in the mps softc.
mps_sas.c: o Track SCSI I/O requests on the io_list from the
time of mpssas_action() through mpssas_scsiio_complete().
o Zero out the request structures used for device
removal commands prior to filling them out.
o Once the target reset task management function completes
during device removal processing, assume any SCSI I/O
commands that are still oustanding will never return
from the controller, and process them manually.
Submitted by: gibbs
MFC after: 3 days
- Use the USB stack's builtin clear-stall feature.
- Wrap some long lines.
- Use memcpy() instead of bcopy().
- Use memset() instead of bzero().
- Tested applications:
/usr/ports/audio/fluidsynth
MFC after: 7 days
Approved by: thompsa (mentor)
frame in DM910x controllers. In r67595(more than 10 years ago) it
was replaced to use "Store and Forward" mode and made controller
generate TX completion interrupt for every frame.
any other media configuration. Otherwise some 21143 controller
cannot establish a link. While I'm here remove the PHY
initialization code in dc_setcfg(). Since dc_setcfg() is called
whenever link state is changed, having the PHY initialization code
in dc_setcfg() resulted in continuous link flips.
After driver resets SIA, use default SIA transmit/receive
configuration instead of disabling autosense/autonegotiation.
Otherwise, controller fails to establish a link as well as losing
auto-negotiation capability. For manual media configuration, always
configure 21143 controller with specified media to ensure media
change. This change makes ANA-6922 establish link with/without
auto-negotiation.
While I'm here be more strict on link UP/DOWN detection logic.
Many thanks to marius who fixed several bugs in initial patch and
even tested the patch on a couple of dc(4) controllers.
PR: kern/79262
Reviewed by: marius
Tested by: marius
port, copy SROM information from base softc as well and run SROM
parser again. This change is necessary for some dual port
controllers to make dc(4) correctly detect PHY media based on first
port configuration table.
While I'm here add a check for validity of the base softc before
duplicating SROM contents from base softc. If driver failed to
attach to the first port it can access invalid area.
PR: kern/79262
Reviewed by: marius
as they're likely not entirely correct, but they give people something
to toy with to compare behaviour/performance.
Disable the anti-noise part, as this apparently interferes with
RIFS. I haven't verified this.
packet duration for the ath_rate_sample module.
This doesn't affect the packet TX at all; only how much time the
sample rate module attributes to a completed TX.
VNET socket push back:
try to minimize the number of places where we have to switch vnets
and narrow down the time we stay switched. Add assertions to the
socket code to catch possibly unset vnets as seen in r204147.
While this reduces the number of vnet recursion in some places like
NFS, POSIX local sockets and some netgraph, .. recursions are
impossible to fix.
The current expectations are documented at the beginning of
uipc_socket.c along with the other information there.
Sponsored by: The FreeBSD Foundation
Sponsored by: CK Software GmbH
Reviewed by: jhb
Tested by: zec
Tested by: Mikolaj Golub (to.my.trociny gmail.com)
MFC after: 2 weeks
the larger, aligned write+erase sizes the driver currently implements.
This preserves write behaviour but makes the flash driver usable for things
like a read-only FFS or a geom_uzip/geom_compress .
Note that since GEOM will now return the sector size as being smaller,
writes of sector size/alignment will now fail with an EIO. Code which
writes to the flash device will have to be (for now) manually taught
about the flash write blocksize.
on space for clang and a.out support is only needed for /boot/loader,
they are excess bytes that serve no useful purpose other than to
support really old kernels (FreeBSD < 3.2 or so). Prefer clang
support over support for these old kernels and remove this code. We
gain about 100 bytes of space this way.
Reviewed by: rdivacky@
1) Translate the native signal number in the appropriate Linux signal.
2) Remove bogus code, which can lead to a panic as it calls
kern_sigtimedwait with same ksiginfo.
3) Return the corresponding signal number.
little further. This gets us further on the way to be able to build it
successfully with clang. Using in-tree gcc, this shrinks boot2.bin with
60 bytes, the in-tree clang shaves off 72 bytes, and ToT clang 84 bytes.
Submitted by: rdivacky
Reviewed by: imp
caused link re-negotiation whenever application joins or leaves a
multicast group. If driver is running, it would have established a
link so there is no need to start re-negotiation. The re-negotiation
broke established link which in turn stopped multicast application
working while re-negotiation is in progress.
PR: kern/154667
MFC after: 1 week
vm_map_insert(), the kmem_back() assumption about newly inserted
entry might be broken due to interference of two factors. In the low
memory condition, when vm_page_alloc() returns NULL, supplied map is
unlocked. If another thread performs kmem_malloc() meantime, and its
map entry is placed right next to our thread map entry in the map,
both entries wire count is still 0 and entries are coalesced due to
vm_map_simplify_entry().
Mark new entry with MAP_ENTRY_IN_TRANSITION to prevent coalesce.
Fix some style issues, tighten the assertions to account for
MAP_ENTRY_IN_TRANSITION state.
Reported and tested by: pho
Reviewed by: alc
- Allocate coherent DMA memory for the request/response queue area and
and the FC scratch area.
These changes allow isp(4) to work properly on sparc64 with usage of the
IOMMU streaming buffers enabled.
Approved by: mjacob
MFC after: 2 weeks
Catch a set vnet upon return to user space. This usually
means return paths with CURVNET_RESTORE() missing.
If VNET_DEBUG is turned on we can even tell the function
that did the CURVNET_SET() which is really helpful; else
we print "N/A".
Sponsored by: The FreeBSD Foundation
Sponsored by: CK Software GmbH
Reviewed by: jhb
MFC after: 11 days
While updating Tx stats, already freed node could be referred and cause
page fault. To avoid such panic, spool Tx stats in driver's softc. Then,
on every ratectl interval, grab node though ieee80211_iterate_nodes() and
update ratectl stats.
* Simplify some code in run_iter_func().
* Fix typo
* Use memset instead of bzero (hselasky @)
PR: kern/153938
Submitted by: PseudoCylon <moonlightakkiy@yahoo.ca>
Approved by: thompsa (mentor)
The algorithm is supposed to work as follows:
in order to prevent starvation, when a new client starts being served we
record the start time and reset the counter of bytes served.
We then switch to a new client after a certain amount of time or bytes,
even if the current one still has pending requests.
To avoid charging a new client the time of the first seek,
we start counting time when the first request is served.
Unfortunately a bug in the previous version of the code failed
to set the start time in certain cases, resulting in some processes
exceeding their timeslice.
The fix (in this patch) is trivial, though it took a while to find
out and replicate the bug.
Thanks to Tommaso Caprai for investigating and fixing the problem.
Submitted by: Tommaso Caprai
MFC after: 1 week