Merlin (ar9280) and later were full-reset if they're doing open-loop TX
power control but the TSF wasn't being saved/restored.
Add ar5212SetTsf64() which sets the 64 bit TSF appropriately.
generally tidy up the TX power programming code.
Enforce that the TX power offset for Merlin is -5 dBm, rather than
any other value programmable in the EEPROM. This requires some
further code to be ported over from ath9k, so until that is done
and tested, fail to attach NICs whose TX power offset isn't -5
dBm.
This improves both legacy and HT transmission on my merlin board.
It allows for stable MCS TX up to MCS15.
Specifics:
* Refactor out a bunch of the TX power calibration code -
setting/obtaining the power detector / gain boundaries,
programming the PDADC
* Take the -5 dBm TX power offset into account on Merlin -
"0" in the per-rate TX power register means -5 dBm, not
0 dBm
* When doing OLC
* Enforce min (0) and max (AR5416_MAX_RATE_POWER) when fiddling
with the TX power, to avoid the TX power values from wrapping
when low.
* Implement the 1 dBm cck power offset when doing OLC
* Implement temperature compensation for 2.4ghz mode when doing OLC
* Implement an AR9280 specific TX power calibration routine which
includes the OLC twiddles, leaving the earlier chipset path
(AR5416, AR9160) alone
Whilst here, use these refactored routines for the AR9285 TX power
calibration/programming code and enforce correct overflow/underflow
handling when fiddling with TX power values.
Obtained from: linux ath9k
It defaults to -5 dBm for eeproms earlier than v21.
This apparently only applies to Merlin (AR9280) or later,
earlier 11n chipsets have a power table offset of 0.
All the code in ath9k which checks the power table offset
and takes it into account first ensures the chip is
Merlin or later.
The earlier way of doing debugging would evaluate the function parameters
before calling the HALDEBUG. In the case of detailed register debugging
would mean a -lot- of unneeded register IO and other stuff was going on.
This method evaluates the ath_hal_debug variable before the function
parameters are evaluated, drastically reducing the amount of overhead
enabling HAL debugging during compilation.
* change the BB gating logic to explicitly define which chips are covered;
the ath9k method isn't as clear.
* don't disable the BB gating for now, the ar5416 initvals have it, and the
ar9160 initval sets it to 0x0. Figure out why before re-enabling this.
* migrate the Merlin (ar9280) applicable WAR from the Kite (ar9285) code
(which won't get called for Merlin!) and stuff it in here.
It's used to calculate:
* the initial per-rate entries for short/long preamble ACK durations;
* packet durations for TDMA slot decisions;
* RTS/CTS protection durations;
* updating the duration field in the 802.11 frame header
This way invalid durations will generate a warning, prompting for it to be
fixed.
as they're likely not entirely correct, but they give people something
to toy with to compare behaviour/performance.
Disable the anti-noise part, as this apparently interferes with
RIFS. I haven't verified this.
The correct bit to set is 0x1 in the high MAC address byte, not 0x80.
The hardware isn't programmed with that bit (which is the multicast
adress bit.)
The linux ath9k keycache code uses that bit in the MAC as a "this is
a multicast key!" and doesn't set the AR_KEYTABLE_VALID bit.
This tells the hardware the MAC isn't to be used for unicast destination
matching but it can be used for multicast bssid traffic.
This fixes some encryption problems in station mode.
PR: kern/154598
putting descriptors (not buffers) across a 4k page boundary can cause issues.
I've not seen it in production myself but it apparently can cause problems.
So, in preparation for addressing this workaround, (re)-expose the particular
HAL capability bit which marks whether the chipset has support for cross-4k-
boundary transactions or not.
A subsequent commit will modify the descriptor allocation to avoid allocating
descriptor entries that straddle a 4k page boundary.
* The existing radio config code was for the AR5416/AR9160 and missed out
on some of the AR9280 specific stuff. Include said stuff from ath9k.
* Refactor out the gain control settings into a new function, again pilfered
from ath9k.
* Use the analog register RMW macro when touching analog registers.
Obtained from: Linux ath9k
TX chainmask.
since the upper layers don't (yet) know about the active TX/RX chainmasks,
it can't tell the rate scenario functions what to use. I'll eventually sort
this out; this restores functionality in the meantime.
The higher levels (net80211, if_ath, ath_rate) need this to make correct
choices about what MCS capabilities to advertise and what MCS rates are
able to be TXed.
In summary:
* AR5416 - 2/3 antennas, 2x2 streams
* AR9160 - 2/3 antennas, 2x2 streams
* AR9220 - 2 antennas, 2x2 sstraems
* AR9280 - 2 antennas, 2x2 streams
* AR9285 - 2 antennas but with antenna diversity, 1x1 stream
After inspecting the ath9k source, it seems the AR5416 and later MACs
don't take an explicit RTS/CTS duration. A per-scenario (ie, what multi-
rate retry became) rts/cts control flag and packet duration is provided;
the hardware then apparently fills in whatever details are required.
The per-rate sp/lpack duration calculation just isn't used anywhere
in the ath9k TX packet length calculations.
The burst duration register controls something different; it seems to
be involved with RTS/CTS protection of 11n aggregate frames and is set
via a call to ar5416Set11nBurstDuration().
I've done some light testing with rts/cts protected frames and nothing
seems to break; but this may break said RTS/CTS and CTS-to-self protection.
Each different radio chipset has a different "good" range of CCA
(clear channel access) parameters where, if you write something
out of range, it's possible the radio will go deaf.
Also, since apparently occasionally reading the NF calibration
returns "wrong" values, so enforce those limits on what is being
written into the CCA register.
Write a default value if there's no history available.
This isn't the case right now but it may be later on when "off-channel"
scanning occurs without init'ing or changing the NF history buffer.
(As each channel may have a different noise floor; so scanning or
other off-channel activity shouldn't affect the NF history of
the current channel.)
* I messed up a couple of things in if_athvar.h; so fix that.
* Undo some guesswork done in ar5416Set11nRateScenario() and introduce a
flags parameter which lets the caller set a few things. To begin with,
this includes whether to do RTS or CTS protection.
* If both RTS and CTS is set, only do RTS. Both RTS and CTS shouldn't be
set on a frame.
This will eventually be used by rate control modules and by the TX
code for calculating packet duration when handling rts/cts protection.
Obtained from: sam@, rpaulo@, linux ath9k
The defaults enabled three chains on the AR5416 even if the card has two
chains. This restores that and ensures that only the correct TX/RX
chainmasks are used.
When HT modes are enabled, all TX chains will be correctly enabled.
This should now enable analog chain swapping with 2-chain cards.
I'm not sure if this is needed for just the AR5416 or whether
it also applies to AR9160, AR9280 and AR9287 (later on); I'll have
to get clarification.
This, along with an initval change which will appear in a subsequent commit,
fixes bus panics that I have been seing with the AR9220 on a Routerstation Pro
(AR7161 MIPS board.)
Obtained from: Linux ath9k
PR: kern/154220
ath9k does a few different things here during config - if it's an early
AR5416 with two chains, it enables all three chains for calibration and
then restores the chainmask to the original values after initial
calibration has completed.
The reason behind this commit is to begin breaking out the chainmask
configuration for this specific reason; follow-up commits will add
the chainmask restore in the ar5416Reset() routine.
* Re-do the structure size/component math to make sure the struct matches
the expected size
* Just to be clear that we care about bitmask ordering, revert my previous
change and instead define that macro if we're on big-endian.
It turns out that the V4K eeprom definitions (used by the AR9285 and
its derivatives) is wrong. These values are at least causing issues
on my AR2427.
With this fix (and initvals in a subsequent commit), the AR2427 behaves
a lot better.
Note - there's still significant drift between the ath9k v4k eeprom
init code (again, used by AR9285 and derivatives) and what's in this
tree. That needs to be investigated and resolved.
The linux ath9k driver and (from what I've been told) the atheros reference
driver does this; it then leaves discarding 11n frames to the 802.11 layer.
Whilst I'm here, merge in a fix from ath9k which maintains a turbo register
setting when enabling the 11n register; and remove an un-needed (duplicate)
flag setting.