status register rather than 0. Without this, a single hardware volume
event triggers an interrupt storm.
- Implement hardware volume control for the Maestro chips. This version
only handles the case where both channels are adjusted at the same time.
Reviewed by: cg
- The mixer_hwmute() function can be called when a soundcard receives a
mute request.
- The mixer_hwstep() function can be used to adjust the volume of one or
both channels.
- The 'hw.snd.hwvol_step' sysctl determines the amount that mixer_hwstep()
adjusts the volume by on each call.
- The 'hw.snd.hwvol_mixer' sysctl specifies the mixer device to adjust the
volume on for both functions. The values used correspond to the
SOUNDCARD_MIXER_* constants.
want according to the modes set with the ppc(4) flags. Especially, it
should fix some problems with mode detection of parallel chipsets
configured to EPP but which have timing troubles with the drives. In such
a case, the driver should now fall back to slower modes (PS2, NIBBLE).
WWNs correctly (Again!) - this time for the case that we're not going
to fully init the adapter if isp_init is called (with ISP_CFG_NOINIT
set in options). The pupose for this is to bring the adapter up to
almost ready to go, get info out of NVRAM, but to not start it up- leaving
it until later to actually start things up if wanted (and possibly with
different roles selected).
with the driver locking up under load.
- Restructure so that we use a static pool of commands/FIBs, rather than
allocating them in clusters. The cluster allocation just made things
more complicated, and allowed us to waste more memory in peak load
situations.
- Make queueing macros more like my other drivers. This adds queue stats
for free. Add some debugging to take advantage of this.
- Reimplement the periodic timeout scan. Kick the interrupt handler
and the start routine every scan as well, just to be safe. Track busy
commands properly.
- Bring resource cleanup into line with resource allocation. We should
now clean up correctly after a failed probe/unload/etc.
- Try to start new commands when old ones are completed. We weren't doing
this before, which could lead to deadlock when the controller was full.
- Don't try to build a new command if we have found a deferred command.
This could cause us to lose the deferred command.
- Use diskerr() to report I/O errors.
- Don't bail if the AdapterInfo structure is the wrong size. Some variation
seems to be normal. We need to improve our handing of 2.x firmware sets.
- Improve some comments in an attempt to try to make things clearer.
- Restructure to avoid some warnings.
o Move the ax88190 code to its own function.
o Move all device_method_t, driver_t and DRIVER_MODULE definitions to the
end of files.
o Wrap a few lines > 80 characters.
o Use the same devclass for all ed drivers. This allows machines with
multiple types of cards to have their cards numbered correctly. Before,
you could wind up with two ed0's.
o Protect if_edvar.h from multiple includes because I was there.
modify chn_setblocksize() to pick a default soft-blocksize appropriate to the
sample rate and format in use. it will aim for a power of two size small
enough to generate block sizes of at most 20ms. it will also set the
hard-blocksize taking into account rate/format conversions in use.
update drivers to implement setblocksize correctly:
updated, tested: sb16, emu10k1, maestro, solo
updated, untested: ad1816, ess, mss, sb8, csa
not updated: ds1, es137x, fm801, neomagic, t4dwave, via82c686
i lack hardware to test: ad1816, csa, fm801, neomagic
others will be updated/tested in the next few days.
This is because calls with M_WAIT (now M_TRYWAIT) may not wait
forever when nothing is available for allocation, and may end up
returning NULL. Hopefully we now communicate more of the right thing
to developers and make it very clear that it's necessary to check whether
calls with M_(TRY)WAIT also resulted in a failed allocation.
M_TRYWAIT basically means "try harder, block if necessary, but don't
necessarily wait forever." The time spent blocking is tunable with
the kern.ipc.mbuf_wait sysctl.
M_WAIT is now deprecated but still defined for the next little while.
* Fix a typo in a comment in mbuf.h
* Fix some code that was actually passing the mbuf subsystem's M_WAIT to
malloc(). Made it pass M_WAITOK instead. If we were ever to redefine the
value of the M_WAIT flag, this could have became a big problem.
striped plexes.
Submitted by: des
Don't lock buffers before calls to sdio, sdio does it by itself.
Submitted by: tegge
parityops: Use correct casts when returning error information.
Requested by: Bernd Walter <ticso@cicely8.cicely.de>
Cor Bosman <cor@xs4all.net>
Kai Storbeck <kai@xs4all.net>
Joe Greco <jgreco@ns.sol.net>
Add support for Compaq SMART-2 RAID (idad) as storage
device for Vinum subdisks.
Reported by: Aaron Hill <hillaa@hotmail.com>
ahc_pci.c:
Add detach support.
Make use of soft allocated on our behalf by newbus.
For PCI devices, disable the mapping type we aren't
using for extra protection from rogue code.
aic7xxx_93cx6.c:
aic7xxx_93cx6.h:
Sync perforce IDs.
aic7xxx_freebsd.c:
Capture the eventhandle returned by EVENTHANDER_REGISTER
so we can kill the handler off during detach.
Use AHC_* constants instead of hard coded numbers in a
few more places.
Test PPR option state when deciding to "really" negotiate
when the CAM_NEGOTIATE flag is passed in a CCB.
Make use of core "ahc_pause_and_flushwork" routine in our
timeout handler rather than re-inventing this code.
Cleanup all of our resources (really!) in ahc_platform_free().
We should be all set to become a module now.
Implement the core ahc_detach() routine shared by all of
the FreeBSD front-ends.
aic7xxx_freebsd.h:
Softc storage for our event handler.
Null implementation for the ahc_platform_flushwork() OSM
callback. FreeBSD doesn't need this as XPT callbacks are
safe from all contexts and are done directly in ahc_done().
aic7xxx_inline.h:
Implement new lazy interrupt scheme. To avoid an extra
PCI bus read, we first check our completion queues to
see if any work has completed. If work is available, we
assume that this is the source of the interrupt and skip
reading INTSTAT. Any remaining interrupt status will be
cleared by a second call to the interrupt handler should
the interrupt line still be asserted. This drops the
interrupt handler down to a single PCI bus read in the
common case of I/O completion. This is the same overhead
as in the not so distant past, but the extra sanity of
perforning a PCI read after clearing the command complete
interrupt and before running the completion queue to avoid
missing command complete interrupts added a cycle.
aic7xxx.c:
During initialization, be sure to initialize all scratch
ram locations before they are read to avoid parity errors.
In this case, we use a new function, ahc_unbusy_tcl() to
initialize the scratch ram busy target table.
Replace instances of ahc_index_busy_tcl() used to unbusy
a tcl without looking at the old value with ahc_unbusy_tcl().
Modify ahc_sent_msg so that it can find single byte messages.
ahc_sent_msg is now used to determine if a transfer negotiation
attempt resulted in a bus free.
Be more careful in filtering out only the SCSI interrupts
of interest in ahc_handle_scsiint.
Rearrange interrupt clearing code to ensure that at least
one PCI transaction occurrs after hitting CLRSINT1 and
writting to CLRINT. CLRSINT1 writes take a bit to
take effect, and the re-arrangement provides sufficient
delay to ensure the write to CLRINT is effective. The
old code might report a spurious interrupt on some "fast"
chipsets.
export ahc-update_target_msg_request for use by OSM code.
If a target does not respond to our ATN request, clear
it once we move to a non-message phase. This avoids
sending a MSG_NOOP in some later message out phase.
Use max lun and max target constants instead of
hard-coded values.
Use softc storage built into our device_t under FreeBSD.
Fix a bug in ahc_free() that caused us to delete
resources that were not allocated.
Clean up any tstate/lstate info in ahc_free().
Clear the powerdown state in ahc_reset() so that
registers can be accessed.
Add a preliminary function for pausing the chip and
processing any posted work.
Add a preliminary suspend and resume functions.
aic7xxx.h:
Limit the number of supported luns to 64. We don't
support information unit transfers, so this is the
maximum that makes sense for these chips.
Add a new flag AHC_ALL_INTERRUPTS that forces the
processing of all interrupt state in a single invokation
of ahc_intr(). When the flag is not set, we use the
lazy interrupt handling scheme.
Add data structures to store controller state while
we are suspended.
Use constants instead of hard coded values where appropriate.
Correct some harmless "unsigned/signed" conflicts.
aic7xxx.seq:
Only perform the SCSIBUSL fix on ULTRA2 or newer controllers.
Older controllers seem to be confused by this.
In target mode, ignore PHASEMIS during data phases.
This bit seems to be flakey on U160 controllers acting
in target mode.
aic7xxx_pci.c:
Add support for the 29160C CPCI adapter.
Add definitions for subvendor ID information
available for devices with the "9005" vendor id.
We currently use this information to determine
if a multi-function device doesn't have the second
channel hooked up on a board.
Add rudimentary power mode code so we can put the
controller into the D0 state. In the future this
will be an OSM callback so that in FreeBSD we don't
duplicate functionality provided by the PCI code.
The powerstate code was added after I'd completed
my regression tests on this code.
Only capture "left over BIOS state" if the POWRDN
setting is not set in HCNTRL.
In target mode, don't bother sending incremental
CRC data.
This sould make the system power-off correctly where the howto had
more bits set than RB_POWEROFF, e.g. RB_NOSYNC.
Submitted by: Peter Pentchev <roam@orbitel.bg>
going to hurt sio(4) performance for the time being. As we get closer to
release and have more of the kernel unlocked we can come back to doing
arcane optimizations to workaround the limitations of the sio hardware.
claimed that their Intel NIC is comatose after a warm boot from Windoze.
This is most likely due to the card getting put in the D3 state. This
should bring it back to life.
PCI code. This saves each driver from having to grovel around looking
for the right registers to twiddle.
I should eventually convert the other PCI drivers to do this; for now,
these three are ones which I know need power state handling.
format version number. (userland programs should not need to be
recompiled when the netgraph kernel internal ABI is changed.
Also fix modules that don;t handle the fact that a caller may not supply
a return message pointer. (benign at the moment because the calling code
checks, but that will change)
require the addition of flag 0x80000 to their config line in
pccard.conf(5). This flag is not optional. These Linksys cards will
not be recognized without it.
Reviewed by: imp, iwasaki
this gives us several benefits, including:
* easier extensibility- new optional methods can be added to
ac97/mixer/channel classes without having to fixup every driver.
* forward compatibility for drivers, provided no new mandatory methods are
added.
aicasm is run on the build machine and therefore needs to be
compiled and linked against the headers and libraries (resp)
of the build machine. Since normally the default include
directories are search after any specified on the command
line, make sure we don't accidentally pick up machine
dependent headers from the kernel compile directory by
specifying /usr/include first.
This solves the (cross) build problem for ia64.
Approved by: gibbs
- Remove redundant header-type-specific support in the cardbus pcibus
clone. The bridges don't need this anymore.
- Use pcib_get_bus instead of the deprecated pci_get_secondarybus.
- Implement read/write ivar support for the pccbb, and teach it how
to report its secondary bus number. Save the subsidiary bus number
as well, although we don't use it yet.
- Break out the /dev/pci driver into a separate file.
- Kill the COMPAT_OLDPCI support.
- Make the EISA bridge attach a bit more like the old code; explicitly
check for the existence of eisa0/isa0 and only attach if they don't
already exist. Only make one bus_generic_attach() pass over the
bridge, once both busses are attached. Note that the stupid Intel
bridge's class is entirely unpredictable.
- Add prototypes and re-layout the core PCI modules in line with
current coding standards (not a major whitespace change, just moving
the module data to the top of the file).
- Remove redundant type-2 bridge support from the core PCI code; the
PCI-CardBus code does this itself internally. Remove the now
entirely redundant header-class-specific support, as well as the
secondary and subordinate bus number fields. These are bridge
attributes now.
- Add support for PCI Extended Capabilities.
- Add support for PCI Power Management. The interface currently
allows a driver to query and set the power state of a device.
- Add helper functions to allow drivers to enable/disable busmastering
and the decoding of I/O and memory ranges.
- Use PCI_SLOTMAX and PCI_FUNCMAX rather than magic numbers in some
places.
- Make the PCI-PCI bridge code a little more paranoid about valid
I/O and memory decodes.
- Add some more PCI register definitions for the command and status
registers. Correct another bogus definition for type-1 bridges.
This clears out my outstanding netgraph changes.
There is a netgraph change of design in the offing and this is to some
extent a superset of soem of the new functionality and some of the old
functionality that may be removed.
This code works as before, but allows some new features that I want to
work with and evaluate. It is the basis for a version of netgraph
with integral locking for SMP use.
This is running on my test machine with no new problems :-)
rather than finding our parent pcib and using its PCI_READ_CONFIG
method.
- Fix the defines for the 32-bit I/O decode registers, and properly
process the 16-bit versions. Now we will correctly check that I/O
resources behind the bridge are going to be decoded.
- Bring the quirk for the Orion PCI:PCI bridge in here (since it
seems to want to set the secondary/supplementary bus numbers).
- Use PCI_SLOTMAX rather than a magic number.
the ISA bus.
- Don't expect that a PCI:ISA bridge will have a correct class value;
if we're checking PCI IDs, only depend on these.
This should fix the loss of ISA on machines with PCI:EISA bridges like the
AS4100.
class/subclass, so give up trying to cull the list. Instead, complain
in the bootverbose case, but otherwise just accept that we will have to
carry this list of device IDs around.
- Improve the formatting for devices identified by the database.
- Fix the pcib_route_interrupt method definition, as an old version
snuck in here somehow 8(
- Remove a couple of the vendor/device IDs for PCI:ISA bridges which
correctly identify themselves.
Submitted by: peter
- Move PCI core code to dev/pci.
- Split bridge code out into separate modules.
- Remove the descriptive strings from the bridge drivers. If you
want to know what a device is, use pciconf. Add support for
broadly identifying devices based on class/subclass, and for
parsing a preloaded device identification database so that if
you want to waste the memory, you can identify *anything* we know
about.
- Remove machine-dependant code from the core PCI code. APIC interrupt
mapping is performed by shadowing the intline register in machine-
dependant code.
- Bring interrupt routing support to the Alpha
(although many platforms don't yet support routing or mapping
interrupts entirely correctly). This resulted in spamming
<sys/bus.h> into more places than it really should have gone.
- Put sys/dev on the kernel/modules include path. This avoids
having to change *all* the pci*.h includes.
since ether_ifattach() does it for us. We do need to call ether_ifdetach()
instead of if_detach(). And we don't have to check for ifp->if_name
already being initialized because it never will be in FreeBSD 4.x and
above.
Reviewed by: Warner Losh, Duncan Barclay
infrastructure. It's not perfect, but it's a lot better than what
we've been using so far. The following rules apply to this:
o BSD component names should be capitalised
o Layer names should be taken from the non-CA set for now. We
may elect to add some new BSD-specific layers later.
- Make it possible to turn off selective debugging flags or layers
by listing them in debug.acpi.layer or debug.acpi.level prefixed
with !.
- Fully implement support for avoiding nodes in the ACPI namespace.
Nodes may be listed in the debug.acpi.avoid environment variable;
these nodes and all their children will be ignored (although still
scanned over) by ACPI functions which scan the namespace. Multiple
nodes can be specified, separated by whitespace.
- Implement support for selectively disabling ACPI subsystem components
via the debug.acpi.disable environment variable. The following
components can be disabled:
o bus creation/scanning of the ACPI 'bus'
o children attachment of children to the ACPI 'bus'
o button the acpi_button control-method button driver
o ec the acpi_ec embedded-controller driver
o isa acpi replacement of PnP BIOS for ISA device discovery
o lid the control-method lid switch driver
o pci pci root-bus discovery
o processor CPU power/speed management
o thermal system temperature detection and control
o timer ACPI timecounter
Multiple components may be disabled by specifying their name(s)
separated by whitespace.
- Add support for ioctl registration. ACPI subsystem components may
register ioctl handlers with the /dev/acpi generic ioctl handler,
allowing us to avoid the need for a multitude of /dev/acpi* control
devices, etc.
We must force payload alignment to a longword boundary to make the
alpha happy. This should stop the driver from trapping on the alpha
when the interface is ifconfig'ed (actually, when the first frame is
received).
USB WebCams, using a patch from Peter Housel.
With this change ugen, and with Peter's 'vid' program
in ports/graphics/vid, we can capture single images from USB Cameras
using the OmniVision OV511 chipset (including some models of the
Creative WebCam 3)
NetBSD merged in Peter's patch to their ugen.c file
several months ago, so this brings us back in line.
Submitted by: Peter Housel <housel@acm.org>
http://members.home.com/housel/
Approved by: Nick Hibma
Change a few indentations to tabs.
Change the functions to use ANSI sytle parameters.
This lowers the diffs between our copy of ugen.c and NetBSD's copy
Approved by: Nick Hibma
Add a test against isp->isp_osinfo.islocked prior to trying to see
whether --isp->isp_osinfo.islocked is zero to cause us to unlock
(non-SMPLOCK case).
in the future:
o Remove pcic_softc from pcic_handle and replace it with a void *
o Reduce dependence on accessing softc via a pcic_handle
Minor cleanups:
o Define a macro to count the size of an array and use it.
o Minor whitespace alignment
o make no slots found a printf not a panic.
HID passed in as an argument at all; callers are typically going to be
sending us static strings anyway.
Submitted by: Munehiro Matsuda <haro@tk.kubota.co.jp>
on. So stop failing the attach if the IRQ is unassigned. With this
patch, I can now boot with PNP-OS YES in my BIOS no differently than
PNP-OS NO (which is a good thing since Windows hangs with PNP-OS NO).
Obtained from: msmith
- standardise error reporting for commands
- simplify the driver-to-controller bio transfer
- add bio in/out accounting
- correctly preserve the command ID in twe_ioctl (thanks to joel@3ware)
There is no more TAILQ fifo to harvest the entropy; instead, there
is a circular buffer of constant size (changeable by macro) that
pretty dramatically improves the speed and fixes potential slowdowns-
by-locking.
Also gone are a slew of malloc(9) and free(9) calls; all harvesting
buffers are static.
All-in-all, this is a good performance improvement.
Thanks-to: msmith for the circular buffer concept-code.
(specifically, how many entries we've looked at so far). Maintain
interrupt instrumentation. Use USEC_SLEEP instead of USEC_DELAY in
a number of places (this allows us to drop locks and sleep instead
of spin). Track changes to configuration options for topology preference.
Fix botched order of printout for Channel, Target, Lun.
like the args to the config space accessors these functions replaced.
This reduces the likelyhood of overflow when the args are used in
macros on the alpha. This prevents memory management faults when
probing the pci bus on sables, multias and nonames.
Approved by: dfr
Tested by: Bernd Walter <ticso@cicely8.cicely.de>
- Use ACPI_PHYSICAL_ADDRESS
- RSDT -> XSDT
- FACP -> FADT
- No APIC table support
- Don't install a global EC handler; this has bad side-effects
(it invokes _REG in *all* EC spaces in the namespace!)
- Check for PCI bus instances already existing before adding them
but a hack! Add `flags 0x8000' to the psm driver to enable it.
The psm driver will try to get out of out-of-sync situation
by disabling the mouse and immediately enable it again.
If you are seeing this out-of-sync problem because of an
incompetent(?!) KVM switch, this hack will NOT be good
for you. However, if you are occasionally seeing the
problem because of lost mouse interrupt, this might help.
4) The cardbus CIS code treats the CIS_PTR as a mapping register if
it is mentioned in the CIS. I don't have a spec handy to understand
why the CIS_PTR is mentioned in the CIS, but allocating a memory range
for it is certainly bogus. My patch ignores bar #6 to prevent the
mapping.
[The pccard spec says that BAR 0 and 7 (-1 and 6 in thic case since we
did a minus one) is "reserved". The off by 1 error has been fixed.
also bar=5 is invalid for IO maps, so we check it.]
5) The CIS code allocated duplicate resources to those already found
by cardbus_add_resources(). The fix is to pass in the bar computed
from the CIS instead of the particular resource ID for that bar,
so bus_generic_alloc_resource succeeds in finding the old resource.
[fixed, also removed superfluous (and incorrect) writing back to the
PCI config space.]
7) The CIS code seems to use the wrong bit to determine rather a particular
register mapping is for I/O or memory space. From looking at the
two cards I have, it seems TPL_BAR_REG_AS should be 0x10 instead
of 0x08. Otherwise, all registers that should be I/O mapped gain
a second mapping in memory space.
[Oops, the spec does say 0x10..., fixed]
Submitted by: Justin Gibbs
Fix amr_map_command so that 40LD-specific commands get the scatter-gather
list count in the right place. I don't understand why AMI did it like
this, but now the AMI MegaManager can talk to the newer (1600 and later)
controllers.
Remove an unused variable.
Include <machine/clock.h> when necessary.
Tweak some debugging levels to make things more intelligible.
io or memory space access enabled. This patch defers the setting
of these bits until after all of the mapping registers are probed.
It might be even better to defer this until a particular mapping
is activated and to disable that type of access when a new
register is activated.
2) The PCI spec is very explicit about how mapping registers and
the expansion ROM mapping register should be probed. This patch
makes cardbus_add_map() follow the spec.
3) The PCI spec allows a device to use the same address decoder for
expansion ROM access as is used for memory mapped register access.
This patch carefully enables and disables ROM access along with
resource (de)activiation.
This doesn't include the prefetching detection stuff (maybe later when code is written to actually turn on prefetching). It also does not use the PCI definitions (yet, I'll try to put this in all at once later)
Submitted by: Justin T. Gibbs
- Make pccbb/cardbus kld loadable and unloadable.
- Make pccbb/cardbus use the power interface from pccard instead of inventing its own.
- some other minor fixes
call instead.
This makes a pretty dramatic difference to the amount of work that
the harvester needs to do - it is much friendlier on the system.
(80386 and 80486 class machines will notice little, as the new
get_cyclecounter() call is a wrapper round nanotime(9) for them).
the interface to use callout_* instead of timeout(). Also add an
IS_MPSAFE #define (currently off) which will mark the driver as mpsafe
to the upper layers.
before adding/removing packets from the queue. Also, the if_obytes and
if_omcasts fields should only be manipulated under protection of the mutex.
IF_ENQUEUE, IF_PREPEND, and IF_DEQUEUE perform all necessary locking on
the queue. An IF_LOCK macro is provided, as well as the old (mutex-less)
versions of the macros in the form _IF_ENQUEUE, _IF_QFULL, for code which
needs them, but their use is discouraged.
Two new macros are introduced: IF_DRAIN() to drain a queue, and IF_HANDOFF,
which takes care of locking/enqueue, and also statistics updating/start
if necessary.
using a cardbus based system with pccbb providing the pcic interface).
Something isn't quite right.. when the driver allocates and activates
its resources, the IO space that was requested reads as all zeros (versus
the original 0xff's as it normally is when there is no device responding).
Also, deactivate the resources before releasing them. OLDCARD doesn't
seem to care but NEWCARD/CARDBUS get rather unhappy if you release
a resource that hasn't been deactivated yet.
Make pcic_p.c only compile with oldcard kernels.
instead of ng_send_data().
The latter could lead to running the IP stack at splimp
instead of splnet, (among other problems) (that MAY be safe
but I wouldn't count on it).
Noticed while preparing a new set of netgraph stuff.
This makes crash recovery work for stripe sizes that are not multiples of
DEFAULT_REVIVE_BLOCKSIZE (currently 64 kB).
While we're here, fix a few cosmetic nits.
Reviewed by: grog
Sponsored by: Enitel ASA (http://www.enitel.no/)
of the data structures to include new members that weren't defined in the
manual I have.
I opted to use Doug Ambrisko's WEP patches since David Cornejo's patches
did not include the necessary changes to ancontrol(8) to actually enable
and use WEP.
NOTE: I don't currently have access to an Aironet card, so I can't test
any of this. Everything compiles and close scrutiny doesn't reveal any
obvious problems, but Murphy's Law applies. This means I will probably
leave these changes in -current for a bit longer than usual until I'm
sure they work right.
This allows us to successfully attach early Storage Dimension cards.
Allocate mailboxes for the 742A bellow the 16MB limit. Although these
cards seem to be able to deal with all other types of data anywhere
in a 32bit address space, 24bit addresses are required for mailboxes.
bt_eisa.c:
Add device IDs for all Storage Dimension products I could
find from their web site.
Thanks to Ted Mittelstaed for loaning me the equipment to diagnose
and fix these problems.
The prior version in the tree was repo-copied from Duncan Barclay's
cvs tree.
Also add $FreeBSD$
Submitted by: Duncan Barclay
Committed-via: raylan link with two webgear cards.
boot problems..
However this demands that dangerously dedicated disks use an
offset of at least 10 from the start to not overwrite the
raid config sector on the HPT...
Shutdown the card when a catastrophic error occurs. This quenches
any interrupts stemming from the card.
aic7xxx_inline.h:
Return instead of processing additional interrupt state
after handling a catastrophic error. We now shutdown the
chip in this case in the hopes that the system can live
without this controller. The shutdown process invalidates any
other interrupt state.
aic7xxx.seq:
Only attempt to clear SCSIBUSL on Ultra2 controllers. The
clearing is workaround for a selection timeout bug on U2/U160
controllers and happens to be illegal on aic7770 (EISA/VL)
controllers.
numerous error recovery buglets.
Many thanks to Tor Egge for his assistance in diagnosing problems with
the error recovery code.
aic7xxx.c:
Report missed bus free events using their own sequencer interrupt
code to avoid confusion with other "bad phase" interrupts.
Remove a delay used in debugging. This delay could only be hit
in certain, very extreme, error recovery scenarios.
Handle transceiver state changes correctly. You can now
plug an SE device into a hot-plug LVD bus without hanging
the controller.
When stepping through a critical section, panic if we step
more than a reasonable number of times.
After a bus reset, disable bus reset interupts until we either
our first attempt to (re)select another device, or another device
attemps to select us. This removes the need to busy wait in
kernel for the scsi reset line to fall yet still ensures we
see any reset events that impact the state of either our initiator
or target roles. Before this change, we had the potential of
servicing a "storm" of reset interrupts if the reset line was
held for a significant amount of time.
Indicate the current sequencer address whenever we dump the
card's state.
aic7xxx.reg:
Transceiver state change register definitions.
Add the missed bussfree sequencer interrupt code.
Re-enable the scsi reset interrupt if it has been
disabled before every attempt to (re)select a device
and when we have been selected as a target.
When being (re)selected, check to see if the selection
dissappeared just after we enabled our bus free interrupt.
If the bus has gone free again, go back to the idle loop
and wait for another selection.
Note two locations where we should change our behavior
if ATN is still raised. If ATN is raised during the
presentation of a command complete or disconnect message,
we should ignore the message and expect the target to put
us in msgout phase. We don't currently do this as it
requires some code re-arrangement so that critical sections
can be properly placed around our handling of these two
events. Otherwise, we cannot guarantee that the check of
ATN is atomic relative to our acking of the message in
byte (the kernel could assert ATN).
Only set the IDENTIFY_SEEN flag after we have settled
on the SCB for this transaction. The kernel looks at
this flag before assuming that SCB_TAG is valid. This
avoids confusion during certain types of error recovery.
Add a critical section around findSCB. We cannot allow
the kernel to remove an entry from the disconnected
list while we are traversing it. Ditto for get_free_or_disc_scb.
aic7xxx_freebsd.c:
Only assume that SCB_TAG is accurate if IDENTIFY_SEEN is
set in SEQ_FLAGS.
Fix a typo that caused us to execute some code for the
non-SCB paging case when paging SCBs. This only occurred
during error recovery.
As of this patchset, the loader builds (under NetBSD/macppc), boots, interacts
and talks to BOOTP/NFS servers.
(main.c was moved from boot/ofw/libofw to boot/ofw/common but has no revision
history)
Reviewed by: obrien
This code has help us comprehence ACPI spec .
Contributors of this code is as follows(except for FreeBSD commiter):
Yasuo Yokoyama,
Munehiro Matsuda,
and ALL acpi-jp@jp.freebsd.org people.
Thanks.
R.I.P.
When the printer is turned off the pipe write will cause and error,
which causes lpd to close the device and reopen it to clear the error.
After a short while the device will disappear from the bus but lpd will
have opened the ulpt0 port by then. ulpt_status will check for status
without checking the sc->dying flag and panic the kernel when the device
finally disappears from the bus.
Submitted by: Ian Dowse <iedowse@maths.tcd.ie>
also
- sync with netbsd
- fix a bug that miscalculates tx cell counts when the pointer size isn't 4
tested both ENI and Adaptec cards on both i386 and alpha.
interface. In addition to using newbus, it also uses bus_space rather
than inb/outb to make it MI. The grody static softc allocation stuff
has been removed as well.
When restarting the sequencer, ensure that the SCBCNT register
is 0. A non-zero count will prevent the setting of the CCSCBDIR
bit in any future dma operations. The only time CCSCBCNT would
be non-zero is if we happened to halt the dma during a reset,
but even that should never happen. Better safe than sorry.
When a command completes before the target responds to an
ATN for a recovery command, we now notify the kernel so that
any recovery operation requeued in the qinfifo can be removed
safely. In the past, we did this in ahc_done(), but ahc_done()
may be called without the card paused. This also avoids a
recursive call to ahc_search_qinifo() which could have occurred if
ahc_search_qinififo() happened to be the routine to complete
a recovery action.
Fix 8bit math used for adjusting the qinfifo. The index must
be wrapped properly within the 256 entry array. We rely on the
fact that qinfifonext is a uint8_t in most cases to handle
this wrap, but we missed a few spots where the resultant
calculation was promoted to an int.
Change the way that we deal with aborting the first or second
entry from the qinfifo. We now swap the first entry in the
qinfifo with the "next queued scb" to force the sequencer
to see an abort collision if we ever touch the qinififo while
the sequencer is mid SCB dma.
aic7xxx.reg:
Add new MKMSG_FAILED sequencer interrupt. This displaced
the BOGUS_TAG interrupt used in some previous sequencer code
debugging.
aic7xxx.seq:
Increment our position in the qinfifo only once the dma
is complete and we have verified that the queue has not
been changed during our DMA. This simplifies code in the
kernel.
Protect against "instruction creep" when issuing a pausing
sequencer interrupt. On at least the 7890/91/96/97, the
sequencer will coast after issuing the interrupt for up
to two instructions. In the past we delt with this by
using carefully placed nops. Now we call a routine to
issue the interrupt followed by a nop and a ret.
Tell the kernel should an SCB complete with the MK_MESSAGE
flag still set. This means the target ignored our ATN request.
Clear the channel twice as we exit the data phase. On the
aic7890/91, the S/G preload logic may require the second
clearing to get the last S/G out of the FIFO.
aic7xxx_freebsd.c:
Don't bother searching the qinfifo for a doubly queued
recovery scb in ahc_done. This case is handled by the
core driver now.
Free the path used to issue async callbacks after the callback
is complete.
aic7xxx_inline.h:
Split the SCB queue routine into a routine that swaps
the SCB with the "next queued SCB" and a routine that
calls the swapping routine and notifies the card of
the new SCB. The swapping routine is now also used by
ahc_search_qinfifo.
circuit generates too much jitter to be used directly as xmit clock.
Don't miscount pending bytes in weird error conditions.
Drop the rest of a packet if we run out of tx-md's.
Trig the xmit-frame signal on rising edge, this fixed the one-bit-too-late
position of the HDLC frames in E1 mode.
pollution in <sys/mutex.h>. This was half fixed in rev.1.3 of
midwayreg.h. The pollution exposed the bug that this driver was using
toy versions of the bus space macros under FreeBSD. Disabling the
toy versions made this driver compile but dependent on the pollution.
There was still a toy version of bus_space_read_1() in unreachable code.
namespace pollution in <sys/mutex.h>. This was half fixed in rev.1.3
of midwayreg.h. The pollution exposed the bug that this driver was
using toy versions of the bus space macros under FreeBSD. Disabling
the toy versions made this driver compile and maybe support PIO space,
but dependent on the pollution.
them. If we leave garbage in them, the dc_apply_fixup() routine may
try to follow bogus pointers when applying the reset fixup.
Noticed by: Andrew Gallatin
Xtal reference instead of the CLADI input.
In unframed E1 mode, tie SIGFRZ low so that the mysycc doesn't
get confused.
Don't mask errors with OOF. Don't ignore OOF errors.
Stop the channel before freeing mbufs in disconnect.
I still have no T1 devices to test with, so the T1 code is non-existent.
multicast filter on the Pegasus chip. Since IPv6 depends a lot
on multicasting, this caused several failures for people trying to
use IPv6 with Pegasus USB ethernet devices.
Submitted by: Jun Kuriyama <kuriyama@FreeBSD.org>